Originally posted by Joshb556
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However for reasons unknown to me I tried one final time without biasing and it fell into place, it wasn't perfect though. Bridge was dead nuts flat on intake cam but lifted approximately .15-.2mm on intake side of head when testing exhaust cam.
Just said fuck it, not going to be perfect and it ended up within spec after all was said and done. Others have gotten their timing nailed down better than I managed on here but I'm sure others have done worse as well.
Glad to hear you resolved it.
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