Today was bushings removal day!
First up were the subframe bushings. During the week Dad had welded up a removal tool. Basically the same concept as the official tool. One end of the tool straddles the subframe surround, around the bushing. A high-tensile threaded rod goes through the bushing, and a plate on the other end of the bushing covers the end face of the bushing. Tighten up the nuts on each end and the bushing is pulled out.
Here's a pic of the tool (complete with demonstration bushing):

And here it is in action:


We basically followed the TIS procedures for the various bushings. The tools that we made for this job mirror the official tools in the way that they work. As you can see in the second photo, we also heated the subframe bushing cages as per the TIS procedure (600C for up to 2 minutes).
Following this process the bushings came out in a reasonably straightforward manner. A fair amount of force needed (as you can see by the design of the tool).
Here's one of the bushings after removal. Not in terrible condition, but also not as great as the new ones going in.

And here's the subframe, free of the 4 main bushings.

:rockband:
Next up was the front diff bushing. Again, a very similar approach here. Just had to make sure we were accurate with the plate that cups the bushing, so that it was small enough to fit into the channel in the subframe, but large enough to cover the outer casing of the bushing.
Here's the tool mid-production:

Dad driving his MIG welder, with plasma cutter in the background. Note that without this equipment (and a parent, or other acquaintance of your choice, who knows how to drive them), manufacture of said bushing removal tools would be very difficult.
And here's a couple of shots showing how the tool fits up.


Note that after these photos were taken, testing proved that we needed to do double-thickness 10mm bar on the crossmember (like the subframe bushing tool) to provide sufficient bend-resistance. Goes to show just how much force is involved. That cross member is 70mm long, and ended up needing to be 20mm thick to take the forces involved!
I didn't actually take any photos of the diff mount bushing during/after removal, but rest assured that we got it out fairly easily.
We celebrated with lunch (which I didn't photograph, and won't show you, cause this is a car forum, not Instagram).
After lunch (which has already taken up too many words in this journal), we moved on to getting the bushings out of the inner ends of the upper and lower control arms.
We spent a while on this. The issue wasn't a mount for the side of the tool the bushing was being pulled towards, we were able to just use a large socket and some steel bar spacers for that (no need to weld up a tool), the issue was finding/manufacturing something the right size to cup the end of the bushing that was being pulled. We messed around with a few designs that we ended up abandoning, because we were in danger of flaring the ends of the aluminium sleeves on the bushings. We then tried just washers, and pulling only the inner core of the bushing, and letting it pull through the rubber. Again, in spite of a lot of force, we weren't able to make it budge even a little bit. At this point we consulted TIS procedure (and this awesome DIY: http://www.m3forum.net/m3forum/showthread.php?t=464146) and determined that we were on the right track, and just needed to apply more force!!!
We wound it back up again, added a pipe extension to the breaker bar, wrapped the whole arrangement in welding gloves in case of catastrophic failure, and just kept cranking. Eventually it gave way, and, once it moves, it's fairly straightforward from there.
No photos of this bit unfortunately, we were a bit focused on not getting hit by flying bits of metal. But basically you just need more force. You have to get to the point where you cannot believe how much force is involved, and then go a few turns beyond that, and that turns out to be enough to make it move :thumbsup2:
Here's a photo magically showing the bushing removed:

We tried the same approach with the lower control arms (using spacers to keep the two halves of the arm with the correct separation). We succeeded in moving the bushing somewhat, but there was so much force involved, and we had zero confidence in being able to reverse the process to get the new ones in, that we decided to cut our losses and buy new arms, which already have the bushing pressed in. At $50 each it's a pretty good deal, and given these are fairly lightweight parts, it's probably good to put new ones on (at least that's what we told ourselves as it got closer to dinner time).
Having already removed the trailing arm bushings a week and a half ago, that brings bushing removal to a closure for us. It's great to have got them all out. It's been really surprising just how much force is required to get the old ones out. Certainly without the ability to manufacture your own tools to get this job done, it would be either very messy and frustrating, or a costly process to get the bushings out.
Tomorrow will be a slower day. It's terrible weather here at the moment, so I'll limit myself to more clean up of the exhaust section 1 and 2.
Over the next few days Dad is going to clean up more parts for painting, and will paint as well if the weather starts playing ball and provides something less that 100% humidity.
Over and out for now.




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