Very big update, not in terms of building the car but moreso in sharing the adventures the car has been on.
So the last update was me at MSRH, and that's where this will post will start off but it is the following weekend. It was miserable out, but a good low stress way to test the car out before heading to Road Atlanta.
MSRH is horrific in the wet, there is a 10-15 mph difference between the wet line and the dry line for corner speed. It is an ice skating ring. So there were many sideways moments, but I have done many laps here so I am comfortable in the wet.
I almost got bit here...
It was just cold and wet but I got a lot of laps in. Car looked like it was ready for the big trip. I put some Direzzas on it since they were on closeout and for peace of mind of new tires for the whole trip. Rear pads were paper so bought some new PFC 08s for that. Also aligned it again. This time I did stock toe for the front, I don't really like the feeling of zero toe, but the main reason was to give the tires best fighting chance for all the highway miles.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrAnyways onto the Roadtrip. Cannonball to Atlanta, in one shot from Houston. Weren't any issues.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrWent to the Aquarium and explored downtown Georgia for a bit. jayjaya29 was nice enough to let me stay at his home and use his workshop to do a bit of trackprep. These 265 Direzzas are significantly wider than the RS4s so we needed to do some fender hammering, as the damage from previous owner wasn't giving it enough clearance.
I knew the car would blow sound at AMP, but I was able to get a couple laps. It was miserable and raining. 107db, is what I got blackflagged for.
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrThat evening I did the SAP delete and did a P/S flush as the system was pretty angry.
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrThen it was time for Road Atlanta. It did dry up after Lunch, but the morning sessions weren't wet. Morning sessions were trouble free.
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrDidn't bother recording with Go Pro. My wife was able to get some external videos.
This event was sold out, so there was a lot of traffic. When it did dry out, I came over turn 3 pretty hard. My instrument cluster did not like this and started acting up all day. Would come in and out, and during one session the tach started touching the oil temp needle so I had to start short shifting. Despite this, I was able to set a new PB, however I was not able to meet my goal of a 1:39.99 here. I had multiple instances where it was showing up on predictable but ran into traffic or cluster would spazz out and distract me.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrBy the end of the day the cluster was struggling. Braking would make it cut out and only work with dimmer at lowest setting. We still had to go to Charleston to see my wifes family I needed to fix it, but I delayed this by a day to give myself time to sort out the cluster. I put out a WTB for a cluster just in case but took it apart at Jay's that night.
I really didn't think it was fixable but luckily was something simple. Please click the Flickr link to see what it was but basically one of the Capacitors had come off the board with the pad.
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrJay was able to repair it for me and cluster was alive again. Also tightened up the shock nut.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrFollowing day, Faustino and I did an impomptu run to Tail of the Dragon. My plan was to head to Charleston that night so we would just go to the Tail do one run and come back.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrEnded up working out perfectly. We had no traffic. Cars didn't really give any trouble, besides mine the power steering had basically no assist at idle after second run.
One of my favorite pics of the car so far.
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrWe ended up heading to Charleston at 3am since I was beat. Needed some sleep. We did Atlanta to Charleston, in one shot. I was on fumes when we got there, and first time ever filling up with 91 in my life. I've always had access to 93.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrAt this point the power steering was crying. Checked the reservoir and yea very bad.
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrTried to do another halfass resevoir flush to bandaid it along but at this point needed a new pump.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrI lucked out, there was a M54 X5 at a Self Service Junkyard.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrI was able to get permission to swap the pump out in a Autozone parking lot. They said I had a hour, I was able to do it in 40 minutes.
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrParked for the night at her Dad's house.
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrRest of the trip was all touristy nothing really car related. Went to Convington, Birmingham and New Orleans.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrTotal trip mileage was about 3000~.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrI was having a brake shudder that was pretty bad felt like a rear rotor. I felt it on way back from Charleston. Not sure what caused it but sure enough. I believe just the Metallurgy of these cheap drilled and slotted rotors. Unfortunately I put another used set on because my friends parts car had them. We traded them some stuff for it.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrFollowing this finally washed the car
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on FlickrI need to fix the cracked wheel so I can have 4 matching wheels.
Also was able to find some NOS PFC 83s for it. Yes you read that right 83, can't imagine how long those have been sitting on the shelf. Threw those in on NYE. Yes I am running the pad clip.
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr
Fall ‘24 Update by Kurvenkamph Motorsport, on Flickr


























































































































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