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heinzboehmer's 2002 Topaz 6MT Coupe

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  • bigjae46
    replied
    Originally posted by heinzboehmer View Post

    Lol, if I didn't want to get this done ASAP, I would 100% take you up on that. A mold for this would fit in the printer, which would make it even easier to make out of CF.
    Yes, a 3D printed mold eliminate the hardest part of making the mold. The only downside is it tends to not be as durable as a composite mold. Only becomes an issue if the plan is to make a LOT of parts.

    Leave a comment:


  • Obioban
    replied
    Originally posted by heinzboehmer View Post

    Lol, if I didn't want to get this done ASAP, I would 100% take you up on that. A mold for this would fit in the printer, which would make it even easier to make out of CF.
    I'm sure this is what you were referring to, but for others benefit...



    I want to start doing this

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  • heinzboehmer
    replied
    Drove my car around for longer today (including a decent chunk of highway driving) and WOW, it drives incredible. Pulling away from a stop and upshifting are buttery smooth now. And it's got torque at super low throttle inputs! Crazy.

    Bryson and I were talking and we can't really come up with a good explanation for why my car wants so much more fuel down low. Maybe I have a vacuum leak or maybe he's got some restriction somewhere or maybe it's the flap? I'll smoke test my car if I can find a tester, but yeah, fairly stumped. Slideways let's flash some stuff on your car and see how it reacts

    Leave a comment:


  • heinzboehmer
    replied
    Originally posted by bigjae46 View Post
    You know what I'm gonna say...I think I can make that in carbon fiber lol
    Lol, if I didn't want to get this done ASAP, I would 100% take you up on that. A mold for this would fit in the printer, which would make it even easier to make out of CF.

    Leave a comment:


  • bigjae46
    replied
    Originally posted by heinzboehmer View Post
    Will this work? Maybe

    Will this crack as soon as I tighten down the vise? Maybe

    Will this shatter as soon as the end mill touches the aluminum? Maybe

    It's unconventional for sure, but I figured I would give it a shot. I did find a bunch of youtube videos of people doing very similar things, so that gives me hope. If it doesn't end up working, I'll have to make/improvise a similar fixture with stiffer materials, so this part will still be very useful to have as a reference.

    I was hoping to get to the machine shop today, but the print isn't ready, so I'll have to go in some day after work next week.
    You know what I'm gonna say...I think I can make that in carbon fiber lol

    Leave a comment:


  • heinzboehmer
    replied
    I engineered cheese:

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    Following the success of the 3D printed front main seal and stud install tools, I decided to see if a 3D printed fixture would work for holding the stock strut bar brackets at the correct angle in the mill.

    Here's some pictures of the fixture without the holes to better show the geometry:

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    Those cuts in the rear are parallel to the strut bar mounting surfaces. Surfaces are fairly flat on the brackets, but there are some casting imperfections:

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    I'm gonna give them the lightest of skims just to get rid of the bumps. The cuts in the fixture will act as a reference when setting them up in the mill. That setup is going to end up being pretty tall, but there's no good way around that thanks to the geometry of these things. If it ends up being too tall, I'll just touch them up on the belt sander instead. Perfect flatness is not crucial here.

    So why make it all swiss cheese-like?

    The answer, counterintuitively, is that the holes add stiffness. This part is way too big to print with 100% infill, so the holes are there to force the slicer to add more walls inside the part. Should drive stiffness up significantly:

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    Will this work? Maybe

    Will this crack as soon as I tighten down the vise? Maybe

    Will this shatter as soon as the end mill touches the aluminum? Maybe

    It's unconventional for sure, but I figured I would give it a shot. I did find a bunch of youtube videos of people doing very similar things, so that gives me hope. If it doesn't end up working, I'll have to make/improvise a similar fixture with stiffer materials, so this part will still be very useful to have as a reference.

    I was hoping to get to the machine shop today, but the print isn't ready, so I'll have to go in some day after work next week.

    Leave a comment:


  • heinzboehmer
    replied
    Originally posted by Bry5on View Post
    Now we’re talking!
    I'm very excited to get all those parts installed.

    I think I'll wait until I get my front triangulation brace installed though. Just in the interest of science.

    Leave a comment:


  • Bry5on
    replied
    Now we’re talking!

    Leave a comment:


  • heinzboehmer
    replied
    Flashed karter16's custom DME FW today to get extra data over CAN and it works perfectly (0x7D0 is the new message):

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    Log of a drive around town immediately after flashing the modified FW: http://datazap.me/u/heinzboehmer/csl...?log=0&data=15

    Thought it was funny that you can see the lack of traction very clearly towards the very end:

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    That's a hard shift from first to second at redline. Note that the slope of the RPM curve is way slower when in second, even though throttle pedal is at WOT. Pink line tells the full story: DSC is kicking in.

    With everything on CAN now, I was able to do multiple rounds of VE tuning without having wires running all throughout the cabin. Just tell gauge.s to start logging, drive around, import logs into tuning spreadsheets, flash car and repeat until satisfied. The only changes I ended up making were down low, but it seems to have resolved essentially all the remaining weirdness. The way it drives now is extremely close to how it drives with the stock airbox + tune.

    Here's the changes that the VE tuning process resulted in, for reference:

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    Extremely happy with how the car is doing these days. Now I need to make the chassis feel as nice as the engine, especially since parts are starting to pile up

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  • heinzboehmer
    replied
    Car is back together. Pretty straight forward, really nothing interesting to share.

    Although I do have to say that my crank holder tool worked great:

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    Also, here's some before and after pics of the front of the engine:

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    Not spotless cause my fingers were really starting to hurt at this point, but it's SO much better. Will at least let me see if there are any other leaks in the future.

    The most disgusting part was by far the AC compressor bracket. Had to pressure wash that one to clean it up:

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    Took it for a spin and it works! No burning oil smell and no leaks that I can see. Car was driving great so I opted to add a decent detour to my test drive just to grab a pretty picture:

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    I'm happy to have gotten this over with. Time to get back to more interesting things!

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  • heinzboehmer
    replied
    Originally posted by Obioban View Post
    That looks unfun. Bet you're glad to have it out.
    Yep no fun at all. Forearms are all cut up and bruised, but so glad to have finished the hard parts. Now it's just a matter of bolting the easy things back together and driving the car.

    Originally posted by bigjae46 View Post
    I may have missed it but where there any symptoms of that dowel pin shearing off?
    Nope! Absolutely zero.

    It's been sheared since before my ownership (so more than 7 years) and has done many, many trips to redline with no issues. Except for the horrible looking mating surfaces, of course.

    Honestly, I can't believe I never thought of finding a replacement for the dowel and fixing it up the first time I found it like this.

    Although, looking back through seven year old pictures, the sprocket looks about as bad as it did a couple days ago:

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  • bigjae46
    replied
    Originally posted by heinzboehmer View Post
    Happy to have gotten the hard parts out of the way. Now just need to get everything reassembled and take the car out for a spin. It's been out of commission for waaay too long.
    I may have missed it but where there any symptoms of that dowel pin shearing off?

    Leave a comment:


  • Obioban
    replied
    That looks unfun. Bet you're glad to have it out.

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  • heinzboehmer
    replied
    First try!

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    ...if you start counting after the second shipments of seals arrived, of course

    Let's backtrack a bit to see how we got here.

    Started by drilling out the dowel in the damper and cleaning up the mating surface. This is what it started out like:

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    Center punched the dowel and it started to move around, so I kinda just kept at it to free it up:

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    Did a bit of drilling and got it out fairly easily. After that, I hit all those super marred/galled (not entirely sure where that built up material is from, if I'm being honest) spots with a dremel and then went over everything with some wet 800 grit. I taped the sandpaper to a large socket to have somewhat of a flat reference for it:

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    Any imperfections that remain are below the mating surface, so they're staying. I did pull the harmonic balancer from my spare engine out of storage to see if I should just use that one instead. Turned out to be a bit rustier than I remember. It needs refinishing and I just have no desire to tackle that additional project right now, so sticking with the one above.

    Next up, I ran the 800 grit around the edge of the crank sprocket to knock off any high spots from all the marring. I also taped some wet 800 grit to the handle of my crank holder tool (it's multiuse!) and used that to quickly skim the mating surface. The marks you see are all below the mating surface, so I decided not to risk getting a dremel near them and just left them alone. Less is more approach for this one:

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    I realize that these parts are in kinda terrible condition, but I just really don't want to take the engine apart any further. Car has 14X,000 mi on it, so the head gasket will likely need to be swapped soon. I plan on taking the timing chain cover off and swapping the sprocket then. Might refresh the spare harmonic balancer I have or just install a new one, we'll see.

    Front main seal installed perfectly on the first try. It did start off a bit crooked, but a quick tap got it squared away. I wish all my previous install attempts had been as easy as this one!

    Last bit of the puzzle was to get the dowel installed. I was able to tap it in most of the way, but the last couple mm required pressing. I installed the damper and finished pressing it in with that. To make sure that it was fully seated and both mating surfaces were making adequate contact, I (terribly) cut some clearance into a piece of paper and put everything together with the paper in between the damper and the crank:

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    Wiggled the paper around as I was tightening the bolts to check if the surfaces had mated or not. It caught as the bolts bottomed out and I wasn't able to wiggle it around any more, nice!

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    And finally, here's the "fixed" crank sprocket:

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    Happy to have gotten the hard parts out of the way. Now just need to get everything reassembled and take the car out for a spin. It's been out of commission for waaay too long.

    Leave a comment:


  • heinzboehmer
    replied
    Originally posted by George Hill View Post
    All I know is it can't be good for the damper to be moving around (which it obviously is by the damage to the crank gear adapter).
    Yeah, most definitely not ideal.

    I'm pretty sure this seal was replaced prior to my ownership. Previous owner mentioned resealing some parts on the front of the engine in an effort to find an oil leak. Oil leak ended up not having anything to do with this seal, but fairly certain it was replaced due to the witness marks on the crank sprocket. Totally possible that whoever replaced it did not torque the bolts to spec or reused them (or both). Fun times.

    Leave a comment:

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