Originally posted by maupineda
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V2 Diff rebuild + Gear Ratio Swap
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Originally posted by maupineda View PostIf I were to use all RD items (same number of steels and clutches), this would give a theoretical value of 18mm!!! no way we can fit all of that in the unit. as mentioned above, the clutch pack gear (what I called spacer gear before) has an effective height of 16mm! More than that and you will likely have a lot of preload and risk the first clutch plate to crack by the piston pump, or wont be able to close the unit at all.
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Originally posted by bigjae46 View Post
I think RD's deal here is the steel/clutch stack will be thicker so it acts like a mechanical clutch diff. The reason being that the viscous pump wears out and no longer engages to the press the clutch stack together. Try reaching out to RD and see if that's normal?
My plan is to go with an OE based layout, that is, clutches and steels, with no spring washer. so I need to stay within reason when assembling my clutch pack.
If you check post #42, you will see that when the washer provided is fully compressed, the clutch stack height calculates to 14.67mm, and about 17.3mm when uncompressed.
OE stack is 14.42mm
There is no information on this, but the pump's piston may have a total travel of 1.5 - 2mm.
If you had a failed viscous pump, even with those spring washers, you wont have a lot more clutch pack material to generate lock VS OE. Without special equipment is tough to say, but I bet the pumps piston takes less force to be pushed in than the force needed to compress the spring washer, if that is the case, the piston will be fully pushed in, and the spring washer will be compressed a bit (but not fully). The issue I see with the RD's approach is that some (I assume most) of the force that the pump generates is used to compress the washer and not to bind the discs & clutches. that is why I wont use any of those spring washers.
I am trying to source 1 more clutch and 2 more steels. if I can do that, this will be my arrayIf not, I plan to reuse 1 clutch, and 2 steels from the OE setup. This will leave me at 15.2mm.Thickness (mm) Qty Height (mm) 1.1 6 6.6 1.03 6 6.18 2.02 1 2.02 Total 14.8
We'll see.Last edited by maupineda; 03-17-2025, 12:29 PM.
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Originally posted by maupineda View Postas mentioned above, the clutch pack gear (what I called spacer gear before) has an effective height of 16mm! More than that and you will likely have a lot of preload and risk the first clutch plate to crack by the piston pump, or wont be able to close the unit at all.
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OE stack is 14.42mm
Another reason to keep the pump at the factory position: lower or higher position will cause the R side-gear to have less or more backlash from the stock.
This means if you don't use the spring washer on the new RD clutch stack then you have to select the right flat shim to have a proper break away torque, through trial-error. Selecting the proper shim is a long process with many thin shims, or many different shim thickness. I think the factory has a magic total clutches + shim thickness and they just need to sort this out without the need to trial-error for the breakaway torque. This magic number is a little higher than 14.42mm based on your measurement of the old worn stack.
Those rebuilt diffs using RD parts with the spring washer will not provide the same locking characteristic as the OEM diff, because the spring absorbs part of the force from the pump instead of transfer 100% of the pump to press on the clutch stack.
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I reassembled the carrier unit without the clutch pack to measure the space between the pump piston and the base plate that supports the clutch stack.
As I had suspected, when removed, the pump piston extends to what I assume is it most extended position. As you can see, there is only ~13mm in between, which means that any clutch stack of 13+ mm will have the piston in its operating range. Without drawing is impossible to know what is the full travel, and although I could press it on the hydro press until it bottoms out and measure, I don’t want to break it.
This explains why there were no shims, possibly not needed, and although I saw in one of the recent RD videos, at least my car had no shims between the piston and the first steel plate.
with my OE clutch pack the pump’s piston would be pressed in around 1.4mm.
RD sold me some extra steel plates and 1 clutch, so my stack will be 0.4mm thicker (14.8 v 14.4) which should be ok assuming the pump has enough travel.
i Also measure the axial displacement of the bottom side gear and it was 8thou, or 0.2mm. I will add. 0.1mm shim.
Last edited by maupineda; 03-21-2025, 05:04 AM.
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Originally posted by maupineda View Posti Also measure the axial displacement of the bottom side gear and it was 8thou, or 0.2mm. I will add. 0.1mm shim.
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I have been playing with the shimming for the short output shaft side gear, I started with a 0.1mm shim, and I reduced the backlash some, but by feel it did not seem to do much. Then I tried 4 shims and with 0.4, the locating shafts don’t go in, with 3 you can get them in if forced, so the happy place is 0.2mm. You can feel thing a bit tighter, there is still lash, but all spins freely.
i will post here the shims I used, they were a bit expensive, but they are hardened to 40 RC which is needed due to the inherit bearing load they will see under use.
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Originally posted by maupineda View PostI have been playing with the shimming for the short output shaft side gear, I started with a 0.1mm shim, and I reduced the backlash some, but by feel it did not seem to do much. Then I tried 4 shims and with 0.4, the locating shafts don’t go in
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