Originally posted by ChapterM3
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THE M3 IS GETTING THE ANRI BUILD TREATMENT - Blown headgasket to build thread
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'09 HP2S, '12 R12GSA, '00 Black 323iT, '02 Alpine 325iT (Track Wagon), '02 Alpine 330iT
Instagram @HillPerformanceBimmers
Email to George@HillPerformance.com
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Wooah, yeah +1 to second opinion. Like George, I don't trust those numbers after seeing that the shop called 35% "good".2002 Topasblau M3 - Coupe - 6MT - Karbonius CSL Airbox - MSS54HP Conversion - Kassel MAP - SSV1 - HJS - PCS Tune - Beisan - MK60 Swap - ZCP Rack - Nogaros - AutoSolutions - 996 Brembos - Slon - CMP - VinceBar - Koni - Eibach - BlueBus - Journal
2012 Alpinweiss 128i - Coupe - 6AT - Slicktop - Manual Seats - Daily - Journal
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Originally posted by Ryan_R View Post
I just pulled this out of my engine a couple weeks ago. Car had no misfires or drivability concerns. Only indications that something was wrong were low dyno numbers (~30hp down from similar setups) and when I did a compression test everything was at 165psi except for cylinder 5 which came in at 145psi.
I don’t mean to scare you, just showing that sometimes bigger issues might not cause a misfire condition.
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Originally posted by George Hill View Post
You need to get a second opinion, seeing these leak down numbers compared to the compression numbers I don't trust either considering your driving observation. 35% on its on is a huge number and for the (4) "good" cylinders to be at that, IDK, I would be skeptical.
Originally posted by heinzboehmer View PostWooah, yeah +1 to second opinion. Like George, I don't trust those numbers after seeing that the shop called 35% "good".
I've been reading that around 5% leak down is considered normal, would you say that's accurate?
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Originally posted by Slideways View PostTheir leak down tester might be off by 30-35% . 120/170 is .70 x 100 is 70%, so those two rear cylinders are down 30% compared to the others.
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A compression tester is like $30 at harbor freight and it's pretty easy test to do, even for a novice mechanic. You only need basic hand tools and you could verify some of the shops data fairly quickly. If you were local, I'd help you out. It's literally 20mins of work from start to finish.
Make sure you pull all the plugs before doing the test so you get true compress and not a false higher reading on 5&6.Last edited by discoelk; 08-31-2023, 02:58 PM.
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Originally posted by discoelk View PostA compression tester is like $30 at harbor freight and it's pretty easy test to do, even for a novice mechanic. You only need basic hand tools and you could verify some of the shops data fairly quickly. If you were local, I'd help you out. It's literally 20mins of work from start to finish.
Make sure you pull all the plugs before doing the test so you get true compress and not a false higher reading on 5&6.
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Originally posted by Halftim3 View PostI believe you need a 12mm adapter, someone correct me if I'm wrong. Also check that the o-rings are in good shape so you get a good seal, should be since your compression tester kit is new, And try to clean the spark plug threads. Good luck 👍
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You should have a 5-10% leakdown percentage. I now don't trust a place that calls 35% good. With how well the engine runs, I wouldn't expect even 35% on the bad cylinders. It may be more expensive but my shop has had decent luck with Cornwell tools. It'll run you $200 to $250 total for a leakdown and compression tester but it's worth having quality tools for this. You can buy straight from their website. This is not something I'd cheap out on because it needs to be accurate.
My head got removed because I wanted to install cams. I found the intake valve seats were all about 1.5mm and intake valves on 4 were very collapsed at almost 2mm with some abnormal wear. The Spec is 1.25mm however I doubt there was an actual issue with sealing just yet. I did a whole head refresh which ran about $4k in labor and parts. I just wanted to put my cams in... but I have to be thorough. I do try to follow my slogan. All sensors(cam, crank, knock, throttle position, temp and preasure) are getting replaced along with vacuum hoses, ICV rubber bits, and any soft item I can manage to get my hands on to replace.
For what it's worth, just about anything can be fixed or replaced. It's just $$$ sometimesLast edited by Arith2; 09-01-2023, 12:02 AM.This is my Unbuild Journal and why we need an oil thread
https://nam3forum.com/forums/forum/m...nbuild-journal
"Do it right once or do it twice"
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I had a HG replacement at 90k miles on my 2003. It cracked between 2 and 3, no misfires, no codes and drove well. It's not until AFTER I did my own HG that I felt the difference. Car was definitely under power.
I drove on my blown HG initially because I couldn't figure out the issue, but I heard sounds in 2nd/3rd/4th @ 2-4k RPM, noticeable only under load, sounded like a bag of marbles. Worse when going up and down the hills of SF. The arching ate a bit of my aluminum head but not substantial enough, the skim cleaned everything right up. I then used a piece of glass with some grit on the bottom block to ensure things are clean and smooth. Vacuum'd up all the debris on the piston's after cleaning them as well.
Long story short, like heinzboehmer said, if you're ever in NorCal there's a group of us that can help get it done in one weekend, this is assuming the machine shop needed to skim your head completes it quickly. My shop took one day to skim and hot tank everything. It's doable and this community can/will help. If there's no space, you can use my 1-car garage to work on it.
Once you're done, you'll realize the actual amount of power you're down even though things "feel" normal. My car was chirping in 1st to 2nd gear after that job, before the job, no dice.
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I want to add to this that while as others have pointed out you should get a proper leak down test done, don’t get your hopes up that your head gasket might actually be fine, it wont be.
My friends car had a blown head gasket too, it drove totally fine, felt fine, didn’t really make any weird noises either, it even went on the dyno, which was the only reason we knew it was down on power. After fitting a new HG and doing a head overhaul it went on the dyno again and made 20hp more.Last edited by bmwfnatic; 09-01-2023, 01:06 PM.E46 ///M3 • 12/2002 • phönix-gelb • 6MT
E39 ///M5 • 12/1998 • avus-blau • 6MT
E60 ///M5 • 11/2006 • saphir-schwarz • 6MT
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Originally posted by Arith2 View PostYou should have a 5-10% leakdown percentage. I now don't trust a place that calls 35% good. With how well the engine runs, I wouldn't expect even 35% on the bad cylinders. It may be more expensive but my shop has had decent luck with Cornwell tools. It'll run you $200 to $250 total for a leakdown and compression tester but it's worth having quality tools for this. You can buy straight from their website. This is not something I'd cheap out on because it needs to be accurate.
My head got removed because I wanted to install cams. I found the intake valve seats were all about 1.5mm and intake valves on 4 were very collapsed at almost 2mm with some abnormal wear. The Spec is 1.25mm however I doubt there was an actual issue with sealing just yet. I did a whole head refresh which ran about $4k in labor and parts. I just wanted to put my cams in... but I have to be thorough. I do try to follow my slogan. All sensors(cam, crank, knock, throttle position, temp and preasure) are getting replaced along with vacuum hoses, ICV rubber bits, and any soft item I can manage to get my hands on to replace.
For what it's worth, just about anything can be fixed or replaced. It's just $$$ sometimes
Originally posted by WestBankM4 View PostI had a HG replacement at 90k miles on my 2003. It cracked between 2 and 3, no misfires, no codes and drove well. It's not until AFTER I did my own HG that I felt the difference. Car was definitely under power.
I drove on my blown HG initially because I couldn't figure out the issue, but I heard sounds in 2nd/3rd/4th @ 2-4k RPM, noticeable only under load, sounded like a bag of marbles. Worse when going up and down the hills of SF. The arching ate a bit of my aluminum head but not substantial enough, the skim cleaned everything right up. I then used a piece of glass with some grit on the bottom block to ensure things are clean and smooth. Vacuum'd up all the debris on the piston's after cleaning them as well.
Long story short, like heinzboehmer said, if you're ever in NorCal there's a group of us that can help get it done in one weekend, this is assuming the machine shop needed to skim your head completes it quickly. My shop took one day to skim and hot tank everything. It's doable and this community can/will help. If there's no space, you can use my 1-car garage to work on it.
Once you're done, you'll realize the actual amount of power you're down even though things "feel" normal. My car was chirping in 1st to 2nd gear after that job, before the job, no dice.
Originally posted by bmwfnatic View PostI want to add to this that while as others have pointed out you should get a proper leak down test done, don’t get your hopes up that your head gasket might actually be fine, it wont be.
My friends car had a blown head gasket too, it drove totally fine, felt fine, didn’t really make any weird noises either, it even went on the dyno, which was the only reason we knew it was down on power. After fitting a new HG and doing a head overhaul it went on the dyno again and made 20hp more.
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October 19, 2023 - UPDATE 3 - THE M3 IS GETTING THE Anri BUILD TREATMENT
Just marking this section in the thread as the beginning of the build. The car will be pick
The car is going to be picked up to start the build this upcoming week of 10.23 - I'll be adding photos and updates all along the way
Stay tuned!
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